Here's what I did last weekend, bike has always seemed to run a bit rich, having tinkered a bit I decided to whip the filter box off and replace all that gubbins with these nice neat cafe racer stylie filters.
The bike has always popped a bit on overrun even after fixing the exhaust leak, so I was a bit perplexed, anyway, when I got to taking the airbox off I found the branch going to the rear cylinder wasn't actually seated properly.
I whipped the box off anyway and fitted the filters, started and ran Ok and found that the choke lever actually did something now it was much leaner, popping got worsebut this was partly expected.
ran it all last week, barks like a rabid dog under acceleration and turned in 60 mpg instead of the usual 50-54 mpg, kept stalling when the throttle was shut off and got a little warmer than usual, plugs went a bit whiter, but not much.
this morning I took the tank off and fiddled with the mixture screws to get the fastest tickover (like it says in the Haynes) then reset the tickover screw to give a good even 1200 rpm tickover and went for a blast.
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yes I am the smugest AT owner, works a treat (I recken it's already been rejetted when the MIG exhaust was put on) runs and sounds like a banshee!!!! mmm nice.



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